Sunday 19 January 2020

Project Snake Update - Jan 2020

Happy New Year to everybody!

I have just realised that it is also just over a year ago that my AK body/chassis kit was delivered.  So it seems like a good point to take stock of where I have got to in the build process.

I also recently discovered that my kit delivery date of 11 January (2019) is the same date as Carroll Shelby's birthday (11 January 1923).  An interesting coincidence!

Delivery Day - 11 January 2019

As it currently stands, I have not made as much progress as I would have liked. The front suspension/axles are complete (minus brakes) but at the rear, I have only got as far as installing the differential.  I had hoped to be at rolling chassis stage by this time.

Front axle complete except for brakes

Rear Differential Unit in place

I have got a lot of the parts for the rear axle prepped and ready to install.  My decision to prep a lot of the parts myself (home sandblasting and powder-coating) took a lot longer than I anticipated (but hopefully saved me a bit of money and added to the satisfaction of doing as much as I can myself).

Rear axle components prepped and powder-coated ready for re-assembly

I have also not really had many opportunities to do much on the build since my last post back in October 2019.  Many things contributed to this.  Work went a bit mental back in the autumn and I spent quite a few weekends having to work rather than play!  We also had some work done on the house (which is still not fully finished), having most of the downstairs floors replaced.  This meant clearing out the contents of all the rooms and a lot of this stuff found its way into the garage, with the result that working space and access to anything was severely hampered.

Even when I did find some time (and make some working space) I found myself thwarted by some unforeseen issues.  I bought myself a 3HP compressor with a 100-litre receiver back in the summer; this performed faultlessly during all the sandblasting that I was doing at the time.  

New compressor - doesn't like the cold...

When I came to try and use the compressor in late autumn, it would not start.  There was a brief humming from the starter before it blew either the fuse in the plug or tripped out the garage power supply!  

I was worried that the starter capacitor was faulty. But after the usual extensive internet-based research, it seems that 3HP is right on the limit of what a domestic electricity supply can provide, especially if the plug is at the end of a long run of cable (such as a garage). Also during cold weather, the overall demand can affect the actual voltage supplied.  Additionally, as the temperature drops the viscosity of the oil in the compressor motor increases.  The result of these factors is that, in colder conditions, the compressor motor can not produce enough power to overcome the higher viscosity of the oil and effectively stalls (and blows the fuse).  

This can be overcome by heating the compressor oil (using a strategically applied heat gun) but took a long time (and spare fuses) before I managed to coax the compressor to turn over.  Hence not a practical solution for trying to do some quick jobs...

Time has not been wasted though.  I have been doing some planning of the next stages, including the brake and fuel line routing and fixing (no ordinary P-clips will be used in this build!) and I am also toying with the idea of utilising an electronic handbrake based on a 12V linear actuator.

Starting to mock-up handbrake set-up in CAD

The next list of jobs to do are:

  • Extract broken screws from one of the rear hubs;
  • Clean and powder-coat ABS rings from rear hubs (these hold the rear axle stub in place);
  • Reassemble rear hubs;
  • Install new universal joints in driveshafts;
  • Install hubs/driveshafts and rear wishbones;
  • Install rear shocks;
  • Cut down rear brake backing plates and powder-coat;
  • Install handbrake shoes and springs in hubs.

The other main development in the progress of Project Snake has been the engine.  My original plan was for a Chevy 6.2L LS3 motor.  This was going to be built by Kyle Rushall.  Kyle and I have been exchanging texts over the past few months about the exact specification of the motor I was after.  In the end, he offered me an alternative engine at a price that I couldn't really refuse.

I'm going to leave you all hanging for the moment as to the final spec, but it will be a 427 cubic inch engine (but not a Ford...), it has titanium con-rods and I need to find somewhere in the confines of the AK body/chassis to locate a dry-sump tank...

A titanium rod - 464 grams compared to over 600 grams for a steel rod

Kyle has started prepping the block and heads.  The engine build should commence around the end of January and is due for completion sometime in March 2020.

The downside is that the new engine is a "bit" more expensive than I had previously budgeted for so I need to rethink spending plans for the next stages while I save up!



Tuesday 3 September 2019

Strippers and Dubious Chemicals

My last few blog posts have dealt with a few "issues" that I have encountered, the outcome of which is that I need to redo the powder coating on a number of parts.

One of the main reasons for powder coating the parts in the first place is that the coating is very durable.  In other words, it's a bugger to remove.  I had a couple of attempts with the sandblaster and various sanding discs and wire wheels; these would eventually remove the majority of the coating but would take a heck of a long time. 

If I lived in the US there would appear to be a number of chemical products available to strip powder coat.  However, none of them are available in the UK.

The internet suggested that, after giving the surface a good abrading to remove the top surface of the coating, paint stripper could be used to remove the remaining powder coat.  Well, normal Nitromors paint stripper had zero effect.

Further research suggested that to be effective, the paint stripper needed to contain a particular chemical ingredient, namely Dichloromethane (DCM).  This was a common solvent many years ago and used to be widely used in paint strippers.  But, probably for good reason, in the modern health and safety-conscious era, it is has been removed from most products.

It took some tracking down but I did manage to find some industrial strength paint stripper containing DCM on the well-known internet auction site and purchased 5 litres.

Innocuous packaging, limited H&S warnings (and no data sheet supplied with the product...)

I need to recoat the rear wishbone spacer tubes and the rear wishbone tie.  I gave these parts a quick session with the angle grinder/flappy wheel combo (and in the case of the wishbone tie, some wire brush treatment to get into the recesses) to scratch up the surface of the powder coat finish.  These were them brushed liberally with the professional strength paint stripper and left to soak for a few minutes.

Health and Safety Tip - DCM paint stripper is potent stuff.  Even outside in well-ventilated conditions, I could smell the solvent content!  Make sure you wear gloves, long sleeves and eye protection.  I got some small splashes on my skin when brushing the stripper on and it starts to burn any exposed skin immediately.  Also, work quickly; this stuff burns even through gloves!  After just a couple of minutes of holding the parts while applying the stripper my fingers were starting to tingle!

The potency does mean that the product is extremely effective.  It only took a few minutes for the surface of the abraded powder coat to start wrinkling and using a wire brush I was able to remove the majority of the original coating.

Less than 5 minutes for paint stripper to do its stuff...

After a wire brushing and rinse off with water

Wishbone tie after flappy wheel/ wire brush treatment

After a few minutes of soaking in paint stripper...

...the majority of old coating could be removed with a wire brush

After rinsing and drying

These parts were then re-prepped for powder coating.  I gave the spacer tubes a thorough going over with the grinder and sanding discs to try and remove as much of the surface pitting as I could.  These and the wishbone tie then had another session in the sandblasting tent before an application of Afterblast.

Wishbone tie after sandblasting...

...and after etching with Afterblast

The wishbone tie was then recoated in Satin Black; this time around I made sure to get a good coating of powder all over the part prior to curing.

Ready for coating (again...)

After curing - better than the first time!

For the wishbone spacer tubes, I tried another approach for the application of the candy red topcoat (another technique sourced from internet research...).  The High Chrome coat was applied and cured as before. This time though, rather than allowing the parts to cool and reheat them prior to applying the candy coat, I tried a technique called 'hot flocking'.  This technique involved applying the second coat to the parts as soon as they were removed from the oven after curing the first coat.  Due to the parts being at or just below curing temperature, the second coat of the powder started to cure as soon as it is applied to the part.  This also meant that the powder adhered far more readily to the part and did not get blown off as easily.  The parts were then cured in the oven as normal for 10 minutes.

Extensive sanding to remove surface pitting

High Chrome coating applied and cured as usual...

...before red candy is 'hot flocked' to parts straight out of the oven

After 10 minutes of curing in the oven

No blemishes and no patchy coating...

Nice result!

The results this time were far better.  The spacer tubes were blemish-free and the consistency of the red candy coat was much more even with no patchy bits. The colour is amazing in the sunlight!

So now I am back on track and I can get on with finishing off cleaning up the rear hubs!

Saturday 31 August 2019

Why You shouldn't rush things...

Sometimes I astound myself with my own stupidity...

If you are up to date with my blog you will recall that I am the proud owner of two rear wishbone ties.

The first one, which I got with the donor axles, was missing the inner bushes.  I used this part as a practice piece for powder coating and as a result, the finish wasn't that great.

The second one, which I got as a replacement, came with the full complement of bushes.  The powder coat finish that I achieved on this part was far better than that of the first tie.

However, it turned out that the first tie was the correct part for my rear axle set-up.  

So my first thought was that I was going to have to re-coat the original wishbone tie, which was going to be a bit of a pain to have to try and strip off the iffy powder coat and get back to bare metal.

Then I had the lightning bolt moment!  Of course, all I had to do was press the inner bushes out of the second wishbone tie.  Then I would have a tie that fitted my rear axle and had a decent finish. Simples!!

Cue another job that should have taken 5 minutes, actually took most of the day and, in this instance, ended in disaster...

Firstly the inner bushes stubbornly refused to budge from the second wishbone tie.  I think I must have almost reached the maximum capacity on my 10-tonne press.  The frame was shaking and the jack was crying hydraulic oil but despite several cycles of loading and unloading the bushes did not even move so much as a millimetre.

A trip to Screwfix to buy a 30mm holesaw for my drill followed, in an attempt to drill out the centre of the bush.  Even this plan of attack was slightly thwarted.  The inner bushes on the wishbone tie are actually 3 sleeves of steel with a rubber sandwich between each.  The resulting thickness of the rubber was thinner than the thickness of the holesaw.  So rather than just cutting through the rubber to allow the inner metal sleeve to be removed, the holesaw had to chew its way through the middle metal sleeve.  This took forever as the saw kept catching and jamming on the end of the metal.  

Eventually, I did manage to work my through the whole of one of the bushes and extract the centre core.  Then all I had to do was gently cut through the outer steel sleeve left in the wishbone housing with a hacksaw and then tap the remains of the bush out. What could go wrong?

Well, two things went wrong.

1) Firstly, rather than secure the wishbone tie in a proper vice, I clamped it into my trusty workmate.  My workmate sits in the corner of my garage; the dark and dimly lit corner.  The constant jamming of the holesaw when trying to drill the bush out kept shaking the tie loose in the workmate.  So I kept tightening it up, tighter and tighter...It was only when I had finished hacksawing out the outer sleeve that I realised that I had not been clamping the wishbone tie by the central (solid) part but on one of the flanges.  My constant tightening of the workbench had distorted the flange inwards.  I tried bending it gently back out and although it straightened out of sorts, it actually bent back from just above the point where the flange was welded onto the main body of the tie.  As a result, I was concerned that the metal had torn slightly above the weld line, rather than bent back to shape (if shape was the right word since the flange still looked quite distorted).

Distinctly "S"-shaped flange - and that was after trying to bend it back...

2) Secondly, my frustration over the whole exercise taking far longer than it should have, resulted in some further carelessness when hacksawing through the outer sleeve.  Rather than set-up a work light to see what I was doing properly I attempted the sawing operation in the aforementioned dark and dim corner of the garage.  After completing the cutting and the outer sleeve popping out onto the floor with a reassuring ping, I released the wishbone tie from the workbench and took it outside to examine my handiwork in a better light.  Of course, I spotted the bent flange at this point but also that I had been too enthusiastic with the hacksaw.  Not only had I cut through the outer sleeve but had managed to cut a sizeable slot into the wishbone tie itself.  

Bush removed - remains of the middle sleeve after operation holesaw on LHS

One inner bush removed.  Looking good...

...except for the addition of a small crack inducer into a highly loaded part...

While I am no mechanical expert, I know enough to realise that the wishbone tie is a highly loaded part of the rear suspension since it is one of the main components transferring the load from the rear suspension into the chassis.  My actions had rendered my spare wishbone tie junk, with a weakened flange and a rather effective crack inducer added to point at which the tie connects to the chassis.

My son has a particular phrase that he used to describe my actions - but I'm not going to repeat it...

So the lesson for today is - even when things are not going to plan, don't rush, take your time and don't cut corners.  It's back to Plan A for me and attempting to re-coat the first wishbone tie...

Powder Coating Fest - Part 3

Having had some reasonably successful results powder coating various donor parts, using either satin black or gloss black powder, I thought it was time to funk things up a bit.

At the 2019 Stoneleigh Kit Car Show, I was looking at the various powder coat colours on the ElectroStaticMagic stand.  I had been contemplating coating a few pieces in either a candy blue or red which would be similar colours to the anodised aeroquip style hose fittings that we plan to use for plumbing Project Snake.

My original thought was to go for a blue candy colour but they didn't have any in stock at the Stoneleigh show so I went for candy red instead (always one for sticking to a plan).  The candy powder is applied over the High Gloss Chrome powder and I picked up 1/4kg of that at the same time.

The first pieces I decided to apply to funk treatment to were the front axle dust caps.  These got the usual wire brushing, sandblasting and Afterblast treatment prior to coating.


Dust Caps - after initial clean...

...after sand blasting

...and after application of Afterblast

The instructions for appying the candy powder coat require an initial coating with the High Chrome powder, which is then cured for 30mins at 180 degrees and then allowed to cool to ambient temperature.  The red candy powder is then applied over the High Chrome and cured for 10mins at 180 degrees.

The dust caps were given a once over with the Eastwood Prepaint Prep and a wipe over with a tack rag and then the High Chrome powder was applied.  This goes on as a flat medium grey colour.


High Chrome powder applied

These were then brought up to temperature in the oven and cured for the recommended 30mins.  The finish of the High Chrome is very good.  The powder cures to an almost chrome-like finish (as the name suggests....).  If leaving the parts as the Chrome finish it is recommended to gloss clear coat the parts to prevent the powder dulling with time.  I reckon this would give the parts a really good shine and, on a well-prepped surface (unlike my battered and bruised dust caps), I think at first glance it would be hard to differentiate the finish from a real chromed part.


Shiny Dust Caps - shame about the dimples...

I can see my face in this one!

Its like looking in a battered mirror....

Next step was to apply the red candy powder.  I did this the day after applying the High Chrome so obviously the parts had cooled completely.  I gave them another wipe over with Prepaint Prep and a tack rag and then tried to apply the red candy powder.  

Note the word 'tried'.  This proved quite tricky.  The second coat of powder didn't want to adhere to the parts at all.  I'm not sure whether I wasn't getting a good ground contact (because of the first coat), although I had scraped a bit of the coating off on the inside where I had placed the hanging/ground wire, but the powder went on in a very patchy manner and when I tried to fill in the gaps, the powder that had coated the part just seemed to blow off.

I ended up blowing all the powder off with an airgun, re-cleaning the parts and trying again.  The second time I turned the air pressure on the powder coating gun down a bit (to around 4psi) and trying to 'fog' the parts in powder.  This did achieve a better coverage (although not a very economic use of powder and everything in the garage now has a slight red tinge to it....) although care was still needed not to blow the powder off in places.


Eventually managed to get parts completely covered...

These were then popped in the oven at 180degrees / Gas mark 4 for 10mins after the parts had reached curing temperature.  I was quite pleased with the results.  The final colour is quite a deep red and so is more like the colour of 'Ruby' (the AK demonstrator that is current inspiration for this project) which is fine assuming we don't change our mind on the final colour!!

Close inspection of the final pieces did show some areas where the coating was a bit patchy, but only if you look closely (and the dust caps will eventually be hidden anyway - which begs the question why did I bother...).  


Freshly cured Candy Red dust caps...

Final result - some minor blemishes!!

Still, it was a good experiment for some parts which might be more visible and so buoyed by the initial success I attempted to powder coat the rear wishbone spacer tubes.

These needed a good session with the angle grinder and some flap wheels to clean off the surface pitting caused by my leaving them too long in a citric acid de-rusting bath previously.  After an intensive session with 40, 80 and then 120 grit flap wheels, the tubes cleaned up quite nicely.



After some flappy wheel treatment...

These then got a final sandblast, spray with Afterblast and a clean up before powder coating with the High Chrome.  As before these were cured at 180 degrees for 30mins.


Chrome coated spacer tubes

Having scoured the internet for some tips on applying the candy powders, I found a couple of tips on various forums, which suggested that, rather than trying to apply the candy powder to a cooled part, it should be preheated to around 65-75 degrees to aid adhesion of the second coat. 

This technique made a big difference and the candy powder seemed to adhere much more readily to the chrome coat, although there were some areas that needed a bit more persuasion than others. 

However, after curing and cooling, I was a bit disappointed with the results.  The candy coat was still quite thin and patchy in places and where I had obviously not managed to remove all the surface blemishes from the tubes with the grinder/flap wheel combo, the powder had concentrated around these giving some very obvious dark spots on the coating.


Patchy coating...


...and dark spots

I know these tubes (and the dust caps) will be hidden from sight once the car is finished, but I still want these bits to be the best finish that they can be.  So at some point soon, I will probably attempt to redo them all.

Tuesday 20 August 2019

Set Blasters to stun.....

Armed with my trusty Budget Blaster Mk2, I had been making good progress with cleaning and prepping many of the donor car parts for powder coating.

However, the change of my blasting media of choice from kiln-dried sand to aluminium oxide soon identified a major issue.  

The aluminium oxide media is far more abrasive than the sand; so abrasive that it actually blew its way through the nozzle of Budget Blaster.  I was starting to notice that it was taking a bit longer to clean off one of the rear hubs and then I spotted the hole in the nozzle...


The additional hole does not improve performance.....

OK I thought, I've managed to do quite a lot of sand blasting with the original nozzle so I'll just order another set of nozzles from a well-known mail-order company that offers next day delivery and that should see me set for a bit longer.  In the meantime, I'll just revert to Budget Blaster Mk1.

A great plan....for less than 5 minutes, by which time Budget Blaster Mk1 had bitten the dust as well.


RIP Budget Blaster Mk1...

Clearly, the nozzles were not going to survive very long with the aluminium oxide media and so I cancelled the order for another set of cheap nozzles and contemplated Plan B.

Plan B involved the purchase of a Clarke SB3 Grit Blasting Gun, the main lure of which was it came with a hardened steel nozzle!  There were fairly mixed reviews of this on the internet, but for £20 I was prepared to give it a go.



Clarke SB3 Grit Blast Gun - photo courtesy of MachineMart

Some of the reviews cited issues with media delivery and volume of media used.  I found one review that said to ensure the delivery tube was fixed facing forwards and to angle the gun downwards in use - which I did and had no problems in use.

However, the speed at which the gun uses blasting media is quite high.  The pot takes has a litre capacity so around 1-1.5kg of media.  My initial experiments with the gun managed to empty a full pot in a couple of minutes.  The results were impressive but clearly, some means of capturing and recycling blast media would be required otherwise 25kg was not going to last very long!

My solution was to buy a large tarpaulin and a cheap gazebo with sides, from the well-known internet auction site, to make a supersize blasting 'cabinet' by laying the tarpaulin on the floor and sitting the gazebo on top.  The theory being that the gazebo would help to contain the excess blast media and this could be swept off the tarpaulin and reused.

For the first full-scale test of this set-up, I reverted to using the kiln-dried sand since a) the damp bag that I bought previously had now dried out a bit and b) if the set-up failed I was only wasting a £3 bag of sand rather than expensive aluminium oxide.  

I have to say the results using the SB3 gun and sand were pretty amazing.  The gun is pretty effective and I managed to strip and clean some of the rear axle parts in less than 30 minutes.  It does go through the media at a phenomenal rate!  But the tarpaulin/gazebo combo did a reasonable job of containing the excess media and with some frequent sweeping up, I did manage to recycle a fair amount of the sand and finished with almost as much as I had started with!

Lifes a Beach - After 5 minutes of blasting...

Initial results...

A quick blast with the aluminium oxide should see these parts finished and ready for powder coating.

So a big thumbs up for Plan B (although unfortunately, the 'B' does not stand for budget...)

Friday 2 August 2019

Differential - Part 3 - I'm a bit tied up at the moment

With the differential fitted and the problems with fitting the wishbone tie resolved, I decided to deviate slightly from the AK build manual instructions.

Rather than press on with installing the rear wishbones and hubs (well my hubs aren't ready in any case), I decided to install the rear differential tie bars.  I had seen from Richard's blog post that he had had some fun and games getting these fitted and I figured it would be easier without all the extra weight of the drivetrain if things needed to be jiggled about!

The AK-supplied tie bars are fixed between two chassis lugs and the upstand flanges on the wishbone tie; one on each side of the chassis.

I offered up the tie bars to the chassis lugs but despite trying both ends of both bars, they did not fit between the lugs.  I find this a bit surprising really; as the tie bars are supplied by AK and the lugs on the chassis are welded on by AK, I would expect the fit to be a bit better.  The difference is more than the thickness of the powder coat and would require some metal removal to allow bushings on tie bar end to fit between the lugs.


Nope - that isn't going to fit!

The simple solution used by many others to this issue has been to reach for the file and file down the ends of the tie bar bushing to fit.  But I don't like removing metal unnecessarily so I went for a different approach.

My plan was to ease the chassis lugs apart very slightly to allow the end of the tie bar to fit between them.  This was achieved using a long bolt passed through the chassis lugs with two nuts installed in between the lugs (with washers under the nuts to protect the powder coat).  Using a couple of spanners to tighten one nut and back off the other, this has the effect of spreading the lugs apart very slightly (I did this very carefully as I didn't want to bend the lugs, just ease them apart).


The patented Acme lug-spreader tool...

I am pleased to say that this actually worked!  Using this approach I managed to spread the lugs sufficiently to be able to tap the end of the tie bar in between the lugs - obviously, the presence of the bolt meant that it only just sat between the lugs.  Then it was a case of gently undoing the nuts on the make-shift lug spreader tool, without disturbing the tie bar.  Then the tie-bar could be gently tapped fully into the lugs and centred over the bolt hole.  To make sure these didn't slip out of position while fixing the differential ends I passed one of the AK-supplied 7/16" by 3" fixing bolts through each of the chassis mounts.

Using this approach I had the chassis ends of both tie bars installed in under an hour - result!

The other ends were much easier, in that the ends of both tie bars fitted between the upstand flanges on the wishbone tie - although the holes did not line up perfectly.  This was easily rectified by loosening the mounting bolts of the wishbone tie which gave enough play to allow the bolt holes to line up.  Again I passed a 7/16" by 3" bolt through each of the holes to hold it in place and tightened the wishbone tie bolts back up again.




First tie bar in place....


....both bars in place

After the fun and games I had had with fixing the wishbone tie, it was good to have a job that I was expecting to take some time only take a couple of hours!

I haven't yet tightened up all the nuts and bolts a) because I need to try and work out from the Haynes manual what all the relevant torque settings are, and b) in case I need to loosen any bits off again to facilitate installation of the rear wishbones and hubs.

I will also probably attempt to re-coat the wishbone tie; since I originally thought this was going to be a spare and I used it for my initial attempts at powder coating, there are some areas that are a bit patchy and thin.  Being the perfectionist that I am I want to get a better finish on this piece - it won't be seen (hidden behind the fuel tank) but I want to minimise the chances of any corrosion developing in future.

I will also probably replace the AK-supplied tie bar mounting bolts with some shorter ones; AK provides 3" long bolts which leaves a significant amount of protruding thread.  I reckon a 2 1/2" or even a 2 1/4" long bolt will look neater.

Now I need to crack on with cleaning up the rear hubs...




Tuesday 16 July 2019

Engine Ordered!

So it appears I have just put down a deposit for my engine!


My plan for the engine is to use a Chevrolet LS3 engine with a Tremec TKO600 transmission. 


My original thought was to buy the engine and gearbox as a complete package from Brian at Roadcraft UK Ltd.  Brian had given me a quote based on the 430hp version of the GM LS3 Crate Engine with all ancillaries and ECU.

I would have preferred the 525hp version of the LS3 Crate Engine, but from reading on the various internet forums it seems there is no chance of this engine passing the IVA emissions test.


At the end of last year another AK Cobra Builder, Barry Boughton, had contacted me after reading my blog.  He recommended the name of a guy, Kyle Rushall, who had built his LS7 engine and also apparently built the engines for Apple and Rufus, the AK Demonstrator vehicles.  I've been in Apple and I can testify to the power the engine in that beast puts out!


Turns out that Kyle used to work at Tim Adams Racing Engines and has built quite a few engines for the Cobra community.  He is now working on his own and building engines for the GT and Drift scene amongst others.  


I made a mental note to drop him a line, but figured that getting a bespoke engine built was always going to be more expensive than buying a crate engine package and never really got round to it. Besides I was planning on spending the rest of 2019 getting the rolling chassis completed and didn't think I would be in a position to need the engine/transmission until early 2020 at best.


Anyway a few weeks ago I saw an advert on Fleabay for an LS7 engine; the price was out of my range but the seller was also offering LS3 engines.  I sent a message asking for prices and it turned out the seller was none other than Kyle Rushall himself!  


He suggested I give him a call to discuss options, which I did and we had a good chat through things.  Turns out he has built a few LS3 engines for Cobra builders now; the last one made over 560hp and passed the IVA test! Not only that but the price he quoted was not a million miles away from what Roadcraft UK was quoting.


Unfortunately, Kyle only has two LS3 cores left and is not expecting to get any more until late 2020.  So after some brief (?!) negotiating with my better half, I have altered by budget plans and put down a deposit to secure one of the remaining cores.
 
The specification for my AK LS3 550 includes

 
  • LS3 Pistons - hot washed and checked
  • Mahle High Performance Piston Rings
  • Custom Camshaft (not too aggressive grind - but guaranteed to pass IVA / MOT)
  • Competition Cams reduced travel Hydraulic Lifters
  • Competition Cams Rocker Trunnion Upgrade (with needle roller bearings)
  • LS3 Conrods
  • ARP High Performance Big End Bolts
  • Clevite Big End Bearings
  • Clevite Mains Bearings
  • MLS Head Gaskets
  • Double Valve Springs
  • Melling Oil Pump
  • Uprated Water Pump
  • New Front Damper
  • New F-body Oil Pan (to fit AK Chassis)
  • New LS3 Intake with 42 lb per hour Injectors
  • One Piece Manley Pushrods
  • New Gaskets
  • New Sensors
  • New Oil Seals
  • Fly-by-Wire Throttle Body
  • Custom Corvette Front End (Power Steering Pump, Alternator, Idler and Custom Tensioner)
  • Canems ECU and Wiring Loom
  • Dyno Run and Set-up
 
Kyle is a busy man and engine won't be ready until later this year, which is fine for me as I still have a way to go to get rolling chassis completed.

I'll have one of those please! (Photo courtesy of Kyle Rushall)